首页 | 本学科首页   官方微博 | 高级检索  
     

一种直流输电无功控制功能优化策略及应用分析
引用本文:周贵勇,郝俊芳,王胜,赵丽莹,史册,王泽宇,于德彬.一种直流输电无功控制功能优化策略及应用分析[J].电力系统保护与控制,2020,48(1):181-187.
作者姓名:周贵勇  郝俊芳  王胜  赵丽莹  史册  王泽宇  于德彬
作者单位:辽宁省电力有限公司检修分公司,辽宁沈阳 110000;许继电气股份有限公司,河南许昌 461000
基金项目:国家重点研发计划项目资助(2016YFB0900600):
摘    要:目前在高压直流输电工程中,当整流站交流系统较弱而要求无功控制功能选择电压控制模式,或无功控制模式处于手动模式时,直流运行中无功控制功能因未配置系统无功平衡控制功能,导致出现交流系统无功越限或不足的问题。现提出一种直流输电工程中无功控制功能的优化策略,并通过RTDS验证了该优化策略的可行性。该策略在高岭背靠背直流工程中实现了首次应用,在确保无功控制功能为手动模式或电压控制模式的同时消除了系统无功越限或不足的问题,提高了直流系统稳定运行效率。

关 键 词:高压直流输电  无功控制  无功越限  电压控制模式  优化策略  高岭
收稿时间:2018/11/26 0:00:00
修稿时间:2019/10/24 0:00:00

Optimization strategy and application analysis of reactive power control function for HVDC transmission
ZHOU Guiyong,HAO Junfang,WANG Sheng,ZHAO Liying,SHI Ce,WANG Zeyu and YU Debin.Optimization strategy and application analysis of reactive power control function for HVDC transmission[J].Power System Protection and Control,2020,48(1):181-187.
Authors:ZHOU Guiyong  HAO Junfang  WANG Sheng  ZHAO Liying  SHI Ce  WANG Zeyu and YU Debin
Affiliation:Overhaul Branch, Liaoning Electric Power Supply Co., Ltd., Shenyang 110000, China,XJ Electric Co., Ltd., Xuchang 461000, China,XJ Electric Co., Ltd., Xuchang 461000, China,Overhaul Branch, Liaoning Electric Power Supply Co., Ltd., Shenyang 110000, China,Overhaul Branch, Liaoning Electric Power Supply Co., Ltd., Shenyang 110000, China,Overhaul Branch, Liaoning Electric Power Supply Co., Ltd., Shenyang 110000, China and Overhaul Branch, Liaoning Electric Power Supply Co., Ltd., Shenyang 110000, China
Abstract:At present,when the reactive power control function in HVDC project is required to select the voltage control mode because of the weaker AC system,or when reactive power control mode is in manual mode and the reactive power control function in DC operation is not equipped with the system reactive power balance control function,the problem of reactive power overstepping or insufficiency in AC system appears.This paper presents an optimization strategy of reactive power control function in HVDC transmission project,and verifies the feasibility of the optimization strategy through RTDS.This strategy has been applied for the first time in Gaolin Back-to-Back HVDC project,eliminating the problem of reactive power exceeding or insufficient while ensuring that the reactive power control function is manual mode or voltage control mode,and improving the stable operation efficiency of DC system.
Keywords:transmission  reactive power control  reactive power overstepping  voltage control mode  optimization strategy  Gaoling
本文献已被 CNKI 维普 万方数据 等数据库收录!
点击此处可从《电力系统保护与控制》浏览原始摘要信息
点击此处可从《电力系统保护与控制》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号