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PTA加氢反应器改造运行状况分析
引用本文:王振新. PTA加氢反应器改造运行状况分析[J]. 合成纤维工业, 2003, 26(1): 49-51
作者姓名:王振新
作者单位:扬子石油化工股份有限公司化工厂,江苏,南京,210048
摘    要:分析了PTA加氢反应器扩能改造的可行性及其效果 ,介绍了改造前后加氢反应系统的运行情况 ,实际生产分析认为 ,加氢反应器单线生产能力由 45 0kt/a扩大至 70 0kt/a后 ,设备运行安全状况得到彻底改变 ,运行经济性及催化剂寿命较原加氢反应器有很大改善 ,优化调整后的工艺参数为配料质量分数 2 7%~2 8%、反应温度 2 82~ 2 83℃、操作压力 7.4~ 7.5MPa、氢气分压 0 .5~ 0 .9MPa ,预计反应系统生产能力可以达到 40 0kt/a。

关 键 词:PTA  加氢精制反应器  改造  运行分析
文章编号:1001-0041(2003)01-0049-03
修稿时间:2002-08-16

Analysis of running situation of PTA hydrogenation reactor after revamping innovation
Wang Zhenxin. Analysis of running situation of PTA hydrogenation reactor after revamping innovation[J]. China Synthetic Fiber Industry, 2003, 26(1): 49-51
Authors:Wang Zhenxin
Abstract:The feasibility and effect of the revamping innovation of PTA hydrogenation reactor were analyzed.The running situation of reaction system before and after innovation was introduced. The practice proved that after the production capacity of hydrogenation reactor was increased from 450 kt/a to 700kt/a, the equipment safety, operation viability and catalyst life were greatly improved as compared with the original hydrogenation reactor. The process parameters were optimized as mass fraction of the feed in the range of 27%~28%, reaction temperature 282~283℃, reaction pressure 7.4~7.5 MPa, hydrogen pressure 0.5~0.9 MPa. The reformed reaction system was expected to be 400 kt/a.
Keywords:PTA  hydrotreating reactor  reform  running analysis  
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