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Improving cost-effectiveness for the furnace in a full-scale refinery plant with reuse of waste tail gas fuel
Authors:Chien-Li Lee  Shuhn-Shyurng Hou  Wen-Jhy Lee  Chih-Ju G Jou
Affiliation:1. Department of Leisure and Recreation Management, Diwan University, Tainan, Taiwan;2. Department of Mechanical Engineering, Kun Shan University, Taiwan;3. Department of Environmental Engineering, National Cheng Kung University, Taiwan;4. Department of Safety, Health and Environmental Engineering, National Kaohsiung First University of Science and Technology, 2, Juoyue Rd., Nantz District, Kaohsiung 811, Taiwan
Abstract:The waste tail gas fuel emitted from refinery plant in Taiwan e.g. catalytic reforming unit, catalytic cracking unit and residue desulfurization unit, was recovered and reused as a replacement fuel. In this study, it was slowly added to the fuel stream of a heater furnace to replace natural gas for powering a full-scale distillation process. The waste tail gas fuel contained on average 60 mol% of hydrogen. On-site experimental results show that both the flame length and orange-yellowish brightness decrease with increasing proportion of waste gas fuel in the original natural gas fuel. Moreover, the adiabatic flame temperature increases as the content of waste gas fuel is increased in the fuel mixture since waste gas fuel has a higher adiabatic flame temperature than that of natural gas. The complete replacement of natural gas by waste gas fuel for a heater furnace operating at 70% loading (i.e. 3.6 × 107 kcal/h of combustion capacity) will save 5.8 × 106 m3 of natural gas consumption, and 3.5 × 104 tons (or 53.4%) of CO2 emission annually. Recovering and reusing the waste tail gas fuel as natural gas replacement will achieve tremendous savings of natural gas usage and effectively lower the emission of carbon dioxide.
Keywords:Waste tail gas fuel  Heater furnace  Carbon dioxide
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