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琼002井尾管胶塞前期损坏的补救措施
引用本文:周向苏,李朝举,聂福贵,雷阿山. 琼002井尾管胶塞前期损坏的补救措施[J]. 石油钻探技术, 1999, 27(1): 33-34
作者姓名:周向苏  李朝举  聂福贵  雷阿山
作者单位:1. 新疆石油管理局塔西南勘探开发公司,新疆泽普,844804
2. 西南石油学院科技开发总公司,四川南充,637100
摘    要:琼002井在尾管固井过程中由于尾管悬挂器长时间地上提下放、旋转等作业,造成尾管胶塞前期损坏,采用TIW型送入工具与Lindsey公司产的回接插入筒组合进行插入式尾管注水泥浆作业,从而很好地解决了尾管胶塞前期损坏的问题。

关 键 词:尾管固井  衬管悬挂器  注水泥用塞  套管损坏  琼002井

A Remedial Measure for Cementing Liner with Damaged Plug in Qiong Well 002
Zhou Xiangsu,Li Chaoju,Nie Fugui,Lei Ashan. A Remedial Measure for Cementing Liner with Damaged Plug in Qiong Well 002[J]. Petroleum Drilling Techniques, 1999, 27(1): 33-34
Authors:Zhou Xiangsu  Li Chaoju  Nie Fugui  Lei Ashan
Abstract:During liner cementing in Qiong Well 002, the liner plug was damaged ahead of time due to liner hanger's long time trips and rotating, so inner pipe cementing was carried using TIW type sending tool along with tieback inserted tubing produced by Lindesy, therefore the problem was solved.
Keywords:liner cementing  liner hanger  cementing plug  casing failure  Qiong Well 002
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