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新安江水电站尾水渠冲刷分析评价
引用本文:王淡善.新安江水电站尾水渠冲刷分析评价[J].大坝与安全,2007(5):48-53.
作者姓名:王淡善
作者单位:华东勘测设计研究院,浙江,杭州,310014
摘    要:新安江大坝已运行40多年,本文通过对水毁情况、历年泄洪情况的分析,并在冲刷坑理论计算和冲坑系数反推分析的基础上,得出冲坑系数在0.62~1.113之间,即使选用较大的可能冲刷深度,大坝、厂房、开关站等主要建筑物的稳定也能得到保证的结论.同时,提出了减轻泄洪对下游冲刷区影响的工程措施.

关 键 词:厂房顶溢流  尾水渠  冲刷  分析  新安江水电站
文章编号:1671-1092(2007)05-0048-06
修稿时间:2007-06-04

Scour analysis and evaluation of tailwater channel at Xin'anjiang hydropower station
WANG Dan-shan.Scour analysis and evaluation of tailwater channel at Xin''''anjiang hydropower station[J].Large Dam & Safety,2007(5):48-53.
Authors:WANG Dan-shan
Affiliation:WANG Dan-shan East China Investigation and Design Institute
Abstract:Xin'anjiang dam has been in operation for more than 40 years.The article elicited that the coefficient of scour hole was between 0.62 and 1.113,even if larger possible scour depth,the stability of main buildings,such as dam,powerhouse and switchyard,can be ensured.Further more,the paper put forward some engineering measures to alleviate flood discharge influence to scour area.
Keywords:overflow type  tailwater channel  scour  analysis  Xin'an jiang hydropower station  
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