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矿渣MTC技术在大港油田的研究应用
引用本文:徐学军,窦同伟,泰建民,徐斌,付友义. 矿渣MTC技术在大港油田的研究应用[J]. 石油钻采工艺, 2004, 26(2): 22-24,25. DOI: 10.3969/j.issn.1000-7393.2004.02.006
作者姓名:徐学军  窦同伟  泰建民  徐斌  付友义
作者单位:1.大港油田集团公司钻采工艺研究院, 天津大港 300280
摘    要:近年来,随着大港油田注水开发程度和井深的进一步增加,地质条件变得更加复杂,采用常规注水泥固井出现顶替效率低、安全窗口窄、易漏失和污染地层等难以解决的问题,给完井和后期增产带来了隐患。为克服这些技术问题,开展了固井水泥浆的室内研究和现场试验。结果表明,矿渣MTC固井技术可针对性地解决大港油田一些区块的固井技术难题,该技术先后在港深14- 22井等14口井中得到应用,固井质量合格率100%,优质率57%,其中油气层段封固优质率达到85%以上,充分说明了矿渣MTC技术可有效地提高复杂区块的固井质量,为后续油井作业环节的顺利开展打下了良好的基础。

关 键 词:大港油田   矿渣MTC   固井技术
收稿时间:2019-05-19

Study on Furnace Slag MTC Technology and Its Application in Dagang Oilfield
by Xu Xuejun,Dou Tongwei,Tai Jianmin,. Study on Furnace Slag MTC Technology and Its Application in Dagang Oilfield[J]. Oil Drilling & Production Technology, 2004, 26(2): 22-24,25. DOI: 10.3969/j.issn.1000-7393.2004.02.006
Authors:by Xu Xuejun  Dou Tongwei  Tai Jianmin  
Affiliation:1.Drilling and Production Research Inst. of Dagang Oilfield Group Company
Abstract:The geological conditions become more complicated in Dagang Oilfield in recent years with the deepening degree of water injection development and hole depth, and the conventional cementing technology is not sufficient for solving the problems erected, such as,low displacement rate,high fluid loss,which causes potential difficulties for completion and stimulation. Lab study and field tests are conducted on the cement slurry system aiming to resolve these technical difficulties. It shows the MTC technology is a good option for the cementing problems in some blocks of Dagang, and it was used in 14 wells such as GS14-22, and cementing qualification rate of 100% and excellent rate of 57% was achieved, and the excellent rate in the pay zone reached as high as 85%.
Keywords:Dagang Oilfield furnace slag MTC cementing technology
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