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砂岩油藏聚合物堵塞机理及解堵方法研究
引用本文:赵林,高申领,陈渊,梅东风,侯宝峰,王瑞,李新丹. 砂岩油藏聚合物堵塞机理及解堵方法研究[J]. 特种油气藏, 2022, 29(3): 156-161. DOI: 10.3969/j.issn.1006-6535.2022.03.023
作者姓名:赵林  高申领  陈渊  梅东风  侯宝峰  王瑞  李新丹
作者单位:1.中国石化河南油田分公司,河南 南阳 473132; 2.中国石油辽河油田分公司,辽宁 盘锦 124109; 3.长江大学,湖北 武汉 430100; 4.油气钻采工程湖北省重点实验室 长江大学,湖北 武汉 430100
基金项目:中国石化科技攻关项目“聚合物驱区块复合解堵技术研究”(P20070-6)
摘    要:针对砂岩油藏聚合物驱过程中聚合物堵塞严重的问题,利用长填砂管多点测压驱替实验和油藏工程方法确定聚合物堵塞半径,利用电镜扫描、CT扫描、核磁共振等手段研究聚合物堵塞机理。结果表明:聚合物堵塞主要发生在靠近填砂管注入端0~1/4处;高渗岩心表面吸附有大量聚合物,聚合物堵塞主要是由吸附引起的,低渗岩心孔径小,孔喉处机械捕集量大,聚合物堵塞主要是由机械捕集引起的;相比于聚合物驱前,聚合物驱后的岩心孔喉平均半径和平均喉道配位数减少,平均孔喉半径由42.2 μm降至39.9 μm,平均喉道配位数由3.36降至3.19。基于堵塞半径和堵塞位置的研究结果,进行了解堵现场试验,解堵后的视吸水指数为解堵前的10.5倍,达到了配注要求。该研究结果可为砂岩油藏聚合物堵塞机理研究和聚合物驱现场试验提供一定的理论指导。

关 键 词:聚合物驱  堵塞位置  堵塞半径  堵塞机理  解堵  砂岩油藏  
收稿时间:2021-07-09

Study on Polymer Plugging Mechanism and Plug Removal Method in Sandstone Reservoirs
Zhao Lin,Gao Shenling,Chen Yuan,Mei Dongfeng,Hou Baofeng,Wang Rui,Li Xindan. Study on Polymer Plugging Mechanism and Plug Removal Method in Sandstone Reservoirs[J]. Special Oil & Gas Reservoirs, 2022, 29(3): 156-161. DOI: 10.3969/j.issn.1006-6535.2022.03.023
Authors:Zhao Lin  Gao Shenling  Chen Yuan  Mei Dongfeng  Hou Baofeng  Wang Rui  Li Xindan
Affiliation:1. SINOPEC Henan Oilfield Company, Nanyang, Henan 473132, China; 2. PetroChina Liaohe Oilfield Company, Panjin, Liaoning 124109, China; 3. Yangtze University, Wuhan, Hubei 430100, China; 4. Hubei Key Laboratory of Drilling and Production Engineering for Oil and Gas, Yangtze University, Wuhan, Hubei 430100, China
Abstract:In order to solve the problem of severe polymer plugging in polymer flooding process in sandstone reservoirs, the polymer plugging radius was determined by the displacement experiment with multi-point pressure measurement of long sand-packed pipe and the reservoir engineering method, and the polymer plugging mechanism was studied by scanning electron microscopy, CT scanning, nuclear magnetic resonance and other methods. The results showed that, polymer plugging mainly occurred at 0-1/4 near the injection end of the sand-packed pipe; a large amount of polymer was adsorbed on the surface of the high-permeability cores, and polymer plugging was mainly caused by adsorption; the pore size of the low-permeability core was small and a great amount of polymer was mechanically captured at the pore throat, and polymer plugging was mainly caused by mechanical capture; compared with that before polymer flooding, the average pore throat radius and average throat coordination number of core after polymer flooding were reduced, with the average pore throat radius reduced from 42.2 μm to 39.9 μm and the average throat coordination number reduced from 3.36 to 3.19. Based on the study results of plugging radius and location, the field test of plug removal was implemented. The apparent water injectivity index after plug removal was 10.5 times that before plug removal, meeting the injection requirements. The results of the study provide theoretical guidance for studying the polymer plugging mechanism in sandstone reservoirs and the field test of polymer flooding.
Keywords:polymer flooding  plugging location  plugging radius  plugging mechanism  unplugging  sandstone reservoir  
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