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新疆呼图壁储气库钻井液技术
引用本文:李称心,高飞,张茂林,王飞,李峰,段利波.新疆呼图壁储气库钻井液技术[J].钻井液与完井液,2012,29(4):45-48,90,91.
作者姓名:李称心  高飞  张茂林  王飞  李峰  段利波
作者单位:1. 西部钻探钻井工程技术研究院,新疆克拉玛依;新疆油田公司开发公司,新疆克拉玛依
2. 新疆油田公司开发公司,新疆克拉玛依
3. 西部钻探准东钻井公司,新疆阜康
4. 西部钻探钻井工程技术研究院,新疆克拉玛依
摘    要:新疆呼图壁储气库井上部井段阻卡频繁,安集海河组泥岩地层易发生剥落、掉块和散塌,三开高密度钻井液由于存在较强的水敏性泥岩污染,维护困难。为减少钻井工程中的复杂事故,采用了强抑制性钻井液体系,包括钾盐钻井液、钾盐-有机盐钻井液、钾盐-双膜屏蔽钻井完井液等,成功解决了各开次钻井液的技术难点,减少了钻井复杂事故,缩短了钻井周期,在目前开钻的10口储气库井中,顺利钻穿安集海河组6口,已完钻3口,其中发生卡钻事故1井次、井漏2井次,完钻井的平均钻井周期为137 d,而以往的勘探开发井发生卡钻15井次、井漏9井次,且阻卡频繁,平均钻井周期为195 d。总结出一系列针对性的技术措施并进行了广泛应用。

关 键 词:储气库井  高密度钻井液  井眼净化  井壁坍塌  防止地层损害  呼图壁区块

Drilling Fluid Technology of Hutubi Gas Storage in Xinjiang
LI Chenxin,Drilling Engineering and Technology Research Institute,West China Drilling and Exploration Co.Ltd.,CNPC,Kalamay,Xinjiang,China GAO Fei,ZHANG Maolin,WANG Fei,LI Feng,DUAN Libo.Drilling Fluid Technology of Hutubi Gas Storage in Xinjiang[J].Drilling Fluid & Completion Fluid,2012,29(4):45-48,90,91.
Authors:LI Chenxin  Drilling Engineering and Technology Research Institute  West China Drilling and Exploration CoLtd  CNPC  Kalamay  Xinjiang  China GAO Fei  ZHANG Maolin  WANG Fei  LI Feng  DUAN Libo
Affiliation:LI Chenxin,Drilling Engineering and Technology Research Institute,West China Drilling and Exploration Co.Ltd.,CNPC,Kalamay,Xinjiang 834000,China GAO Fei,ZHANG Maolin,WANG Fei,LI Feng,DUAN Libo
Abstract:In Hutubi gas storage wells, frequent pipe-stuck, collapsing, and caving are encountered in upper formations,and it is hard to maintain the high density drilling fluid because of contamination by high water-sensitivity mudstone inthe third interval. The high inhibitive capability drilling fluid systems are applied, such as potassium salt drilling fluid,potassium-organic salt drilling fluid, potassium-double membrane shield drill-in fluid systems, to reduce operation terms. Inapplication of 10 wells, 6 of which have drilled through Anjihaihe group safety, and 3 of which are finished. In these wells,there are only one time of pipe-stuck, 9 times of lost circulation, and the drilling period is 137 days, compared with the offsetwells of 15 times of pipe-stuck, 9 times of lost circulation and 195 days drilling period, satisfied result is achieved.
Keywords:Gas storage well  High density drilling fluid  Hole-cleaning  Wellbore caving  Preventing formation damage  Block of Hutubi
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