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曝气生物滤地在污水回用中去除氨氮的试验研究
引用本文:张彪,石晓东.曝气生物滤地在污水回用中去除氨氮的试验研究[J].给水排水,2009,35(Z2).
作者姓名:张彪  石晓东
作者单位:北京金州工程有限公司,北京,100101
摘    要:采用曝气生物滤地(BAF)工艺处理某污水处理厂模拟二级出水,研究了水力负荷及滤料层高度对NH_3-N去除效果的影响.试验结果表明,当进水NH_3-N≤25 mg/L时,平均NH_3-N去除率达到93.12%,出水NH_3-N可降至3 mg/L以下.当水力负荷为1.44 m~3/(m~2·h),HRT为1.8 h时,氨氮的去除效果最好,去除率达到95.32%,出水NH_3-N在1.5 mg/L以下.BAF对NH_3-N的去除作用主要发生在滤料的中上层.

关 键 词:曝气生物滤地(BAF)  二级出水  氨氮  污水处理厂

Experimental study on the treatment of ammonia nitrogen in wastewater reuse by biological aerated filter
Zhang Biao,Shi Xiaodong.Experimental study on the treatment of ammonia nitrogen in wastewater reuse by biological aerated filter[J].Water & Wastewater Engineering,2009,35(Z2).
Authors:Zhang Biao  Shi Xiaodong
Abstract:Secondary effluent of wastewater treatment plant has been treated with the biological aerated filter (BAF) process. Its effects on NH_3-N removal of hydraulic load and height of filter media layer are studied. The results show that biological aerated filter can remove NH_3-N perfectly when NH_3-N concentration of influent≤25 mg/L. The average removal efficiency reaches 93.12%, and NH_3-N concentration of effluent is below 3 mg/L. When hydraulic load is 1.44 m~3/(m~2·h) and hydraulic retention time is 1.8 h, the optimal NH3-N removal efficiency of 95.32% has been got, and NH_3-N concentration of effluent is below 1.5 mg/L. Removal of NH_3-N by BAF mainly occurs in the middle and upper media layer.
Keywords:Biological aerated filter  Secondary effluent  Ammonia nitrogen  Wastewater treatment plant
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