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Unsteady Tip Clearance Flow Pattern in an Isolated Axial Compressor Rotor with Micro Tip Injection
作者单位:Shaojuan Geng Hongwu Zhang Jingyi Chen Weiguang Huang Institute of Engineering Thermophysics,Chinese Academy of Sciences,P.O.Box 2706,Beijing 100080,China Shaojuan Geng:Ph.D.
摘    要:A numerical study of the effect of discrete micro tip injection on unsteady tip clearance flow pattern in an isolatedaxial compressor rotor is presented,intending to better understand the flow mechanism behind stall control meas-ures that act on tip clearance flow.Under the influence of injection the unsteadiness of self-induced tip clearanceflow could be weakened.Also the radial migration of tip clearance vortex is confined to a smaller radial extentnear the rotor tip and the trajectory of tip clearance flow is pushed more downstream,So the injection is benefi-cial to improve compressor stability and increase static pressure rise near rotor tip region.The results of injectionwith different injected mass flow rates show that for the special type of injector adopted in the paper the effect ofinjection on tip clearance flow may be different according to the relative strength between these two streams offlow.For a fixed injected mass flow rate,reducing the injector area to increase injection velocity can improve theeffect of injection on tip clearance flow and thus the compressor stability.A comparison of calculations betweensingle blade passage and multiple blade passages validates the utility of single passage computations to investi-gate the tip clearance flow for the case without injection and its interaction with injected flow for the case with tipinjection.

关 键 词:孤立轴压缩机  插孔  空气间隙流  不稳定性
收稿时间:15 August 2007

Unsteady tip clearance flow pattern in an isolated axial compressor rotor with micro tip injection
Authors:Shaojuan Geng  Hongwu Zhang  Jingyi Chen  Weiguang Huang
Affiliation:(1) Institute of Engineering Thermophysics, Chinese Academy of Sciences, P.O. Box 2706, Beijing, 100080, China
Abstract:A numerical study of the effect of discrete micro tip injection on unsteady tip clearance flow pattern in an isolated axial compressor rotor is presented,intending to better understand the flow mechanism behind stall control meas- ures that act on tip clearance flow.Under the influence of injection the unsteadiness of self-induced tip clearance flow could be weakened.Also the radial migration of tip clearance vortex is confined to a smaller radial extent near the rotor tip and the trajectory of tip clearance flow is pushed more downstream,So the injection is benefi- cial to improve compressor stability and increase static pressure rise near rotor tip region.The results of injection with different injected mass flow rates show that for the special type of injector adopted in the paper the effect of injection on tip clearance flow may be different according to the relative strength between these two streams of flow.For a fixed injected mass flow rate,reducing the injector area to increase injection velocity can improve the effect of injection on tip clearance flow and thus the compressor stability.A comparison of calculations between single blade passage and multiple blade passages validates the utility of single passage computations to investi- gate the tip clearance flow for the case without injection and its interaction with injected flow for the case with tip injection.
Keywords:unsteady tip clearance flow  tip injection  axial compressor  
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