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反渗透(RO)前处理系统SDI优化实践
引用本文:陈刚,张羽翔,宁淑霞.反渗透(RO)前处理系统SDI优化实践[J].华北电力技术,2007(9):30-33,50.
作者姓名:陈刚  张羽翔  宁淑霞
作者单位:新疆电力科学研究院,新疆乌鲁木齐,830000;独山子石化公司热电厂,新疆克拉玛依,833600
摘    要:采用地表水的反渗透系统,经过混凝处理后外观清澈,经砂滤和活性炭过滤后浊度接近0.1 NTU,但污染指数(SD I)仍然在4以上,投运反渗透会导致产水量随时间的增加而递减速度加快,需要高压泵升压维持产水量,使反渗透膜寿命降低。本文就这一问题进行分析并提出了可行的解决方案。

关 键 词:地表水  反渗透(RO)  污染指数(SDI)  混凝  絮凝
文章编号:1003-9171(2007)09-0030-04
修稿时间:2007-04-23

SDI Optimization Practice for Reverse Osmosis Pretreatment System
Chen Gang,Zhang Yu-xiang,Ning Shu-xia.SDI Optimization Practice for Reverse Osmosis Pretreatment System[J].North China Electric Power,2007(9):30-33,50.
Authors:Chen Gang  Zhang Yu-xiang  Ning Shu-xia
Affiliation:1.Xinjiang Electric Power Research Institute;Urumuqi 830000;China;2.Xinjiang Dushanzi Cogeneration Power Plant;Kelamayi 833600;China
Abstract:The ground water with RO pretreatment will be fair clear after coagulation,the turbidity of the ground water is about 0.1 NTU after filtration with mechanical filter and active carbon,but the SDI of the ground water is still in excess of 4,if the RO pretreatment is run,the permeate flux will increase,but the increasing rate will decline with time.The useful time of the RO membrane will reduce,if the permeate flux is maintained with high pressure pump.This article gives the analysis and the solution for the ...
Keywords:ground water  reverse osmosis  slude density index  coagulation  flocculation  
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