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脱水装置醇耗影响因素分析及应对措施
引用本文:卢满生,周红,罗艳,李勇,胡德芬.脱水装置醇耗影响因素分析及应对措施[J].天然气与石油,2011(6):27-29,5.
作者姓名:卢满生  周红  罗艳  李勇  胡德芬
作者单位:中国石油西南油气田公司重庆气矿大竹采输气作业区;中国石油西南油气田公司;渝川燃气有限责任公司;中国石油西南油气田公司重庆气矿工艺研究所;
摘    要:随着气田进入后期开采,气井逐步实施泡沫排水、气举排水、增压等工艺措施,各种措施对下游脱水装置醇耗的影响也日益突显。通过对脱水装置处理气源气质、气量及上游气井实施措施影响进行了深入分析,认为上游来气酸性气质变化、杂质影响、增压运行及润滑油影响、气量调配频繁等是气田后期生产对脱水装置醇耗的主要影响因素。为降低脱水装置醇耗,建议在加强上游气田及脱水装置日常运行管理的同时,采取适当的增压设计,选择适当的过滤分离设备。

关 键 词:脱水装置  醇耗  分析  解决措施

Analysis on Influence Factors of Methanol Consumption of Dehydration Unit and Countermeasures
Lu Mansheng,Li YongZhou Hong,Luo YanHu Defen.Analysis on Influence Factors of Methanol Consumption of Dehydration Unit and Countermeasures[J].Natural Gas and Oil,2011(6):27-29,5.
Authors:Lu Mansheng  Li YongZhou Hong  Luo YanHu Defen
Affiliation:Lu Mansheng,Li Yong(PetroChina Southwest Oil and Gas Company Chongqing Gas Well Area Gas Production and Transportation Dazhu Operation Area,Dazhu,Sichuan,635100,China)Zhou Hong,Luo Yan(PetroChina Southwest Oil and Gas Company Chongqing-Sichuan Gas Co.,Ltd.Chongqing,400021,China)Hu Defen(PetroChina Southwest Oil and Gas Company Chongqing Gas Well Area Technology Research Institute,Chongqing,China)
Abstract:In later stage of gas field development,various kinds of measures,such as foam drainage,gas lift drainage and pressurization,will have significant effects on methanol consumption of downstream dehydration unit.After analysis on quality and volume of gas to be treated in the dehydration unit,it is considered that gas quality,impurity,pressurization,lubricating oil quality and frequent gas volume change are main factors affecting methanol consumption of the dehydration unit in later stage of gas field develop...
Keywords:Dehydration unit  Methanol consumption influence analysis  Solution  
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