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1.
为考察啤酒厂污水处理站的脱水污泥(简称啤酒污泥)用作城市污水厂接种污泥的可行性,摸索污泥的培养与驯化规律,采用连续操作、全流量同步培养和驯化方法,在处理能力为500m^2/d的UNITANK池中对啤酒污泥进行了培养和驯化。试验结果表明,啤酒污泥完全可以作为城市污水处理厂的接种污泥使用,而且培养时间短,出水水质好。曝气0.5h、厌氧搅拌1h时,活性污泥增长最快。将DO控制在2mg/L左右有利于活性污泥的增长;当DO长时间在7mg/L以上时,污泥浓度下降趋势明显。污泥浓度达到2000mg/L所需的培养驯化时间仅为5d;使出水水质达到一级B标准所需的培养时间约为6d。这种培养、驯化方法和经验可为其他城市污水处理厂的建设和运行提供参考。  相似文献   

2.
丝状菌污泥膨胀是影响活性污泥法高效、稳定运行的重要因素。采用A/O生物除磷工艺中试装置处理实际生活污水,分析了污泥膨胀发生的原因及恢复系统性能的方法。结果显示,长期曝气不均匀是导致丝状菌污泥膨胀的重要原因,通过调控系统运行参数可以有效控制由低DO值或者高负荷引起的丝状菌污泥膨胀。当发生污泥膨胀后,首先降低负荷至0.45 kgCOD/(kgMLSS.d),调节回流比为83%,同时控制好氧池各段的DO分别为1.5、1.0、1.0 mg/L以淘汰丝状菌,在SVI值降至200 mL/g以下后继续降低回流比至53%,同时降低曝气量以形成1.0、0.5、0.5 mg/L的DO浓度梯度。采取上述调控措施后,SVI值由569.8 mL/g降至150 mL/g以下,污泥性状得以恢复;同时出水COD和TP分别在50、0.5 mg/L以下,去除率分别约为85%、95%。  相似文献   

3.
Chon DH  Rome M  Kim YM  Park KY  Park C 《Water research》2011,45(18):6021-6029
To investigate the mechanism of sludge reduction in the anaerobic side-stream reactor (SSR) process, activated sludge with five different sludge reduction schemes were studied side-by-side in the laboratory. These are activated sludge with: 1) aerobic SSR, 2) anaerobic SSR, 3) aerobic digester, 4) anaerobic digester, and 5) no sludge wastage. The system with anaerobic SSR (system #2) was the focus of this study and four other systems served as control processes with different functions and purposes. Both mathematical and experimental approaches were made to determine solids retention time (SRT) and sludge yield for the anaerobic SSR process. The results showed that the anaerobic SSR process produced the lowest solids generation, indicating that sludge organic fractions degraded in this system are larger than other systems that possess only aerobic or anaerobic mode. Among three systems that involved long SRT (system #1, #2, and #5), it was only system #2 that showed stable sludge settling and effluent quality, indicating that efficient sludge reduction in this process occurred along with continuous generation of normal sludge flocs. This observation was further supported by batch anaerobic and aerobic digestion data. Batch digestion on sludges collected after 109 days of operation clearly demonstrated that both anaerobically and aerobically digestible materials were removed in activated sludge with anaerobic SSR. In contrast, sludge reduction in the aerobic SSR process or no wastage system was achieved by removal of mainly aerobically digestible materials. All these results led us to conclude that repeating sludge under both feast/fasting and anaerobic/aerobic conditions (i.e., activated sludge with anaerobic SSR) is necessary to achieve the highest biological solids reduction with normal wastewater treatment performance.  相似文献   

4.
Conventional abattoir wastewater treatment processes for carbon and nutrient removal are typically designed and operated with a long sludge retention time (SRT) of 10–20 days, with a relatively high energy demand and physical footprint. The process also generates a considerable amount of waste activated sludge that is not easily degradable due to the long SRT. In this study, an innovative high-rate sequencing batch reactor (SBR) based wastewater treatment process with short SRT and hydraulic retention time (HRT) is developed and characterised. The high-rate SBR process was shown to be most effective with SRT of 2–3 days and HRT of 0.5–1 day, achieving >80% reduction in chemical oxygen demand (COD) and phosphorus and approximately 55% nitrogen removal. A majority of carbon removal (70–80%) was achieved by biomass assimilation and/or accumulation, rather than oxidation. Anaerobic degradability of the sludge generated in the high-rate SBR process was strongly linked to SRT, with measured degradability extent being 85% (2 days SRT), 73% (3 days), and 63% (4 days), but it was not influenced by digestion temperature. However, the rate of degradation for 3 and 4 days SRT sludge was increased by 45% at thermophilic conditions compared to mesophilic conditions. Overall, the treatment process provides a very compact and energy efficient treatment option for highly degradable wastewaters such as meat and food processing, with a substantial space reduction by using smaller reactors and a considerable net energy output through the reduced aerobic oxidation and concurrent increased methane production potential through the efficient sludge digestion.  相似文献   

5.
SVI在Orbal氧化沟运行管理中的指导作用   总被引:1,自引:0,他引:1  
在污水处理厂的实际运行管理中,影响活性污泥处理工艺运行效果的因素很多,在缺乏经验数据的情况下,运行管理人员常以污泥容积指数(SVI)作为指导运行的主要参数。通过对西安市第三污水处理厂Orbal氧化沟工艺在运行中的实测结果进行统计分析,归纳出了SVI与污泥负荷NS、溶解氧DO及出水SS之间的相关关系,提出以SVI值指导Orbal氧化沟的工艺运行。  相似文献   

6.
This work aims to compare biomass structure and performance of a submerged membrane bioreactor (SMBR) and an activated sludge process (ASP) treating the same domestic wastewater. The influence of the separation technique (membrane filtration or settling) and operation at high sludge-retention time (SRT) were investigated. Over the entire range of SRT (10-110 days), the SMBR achieved very good organic removal efficiencies, ranging from 90.8+/-0.2% to 94.2+/-1.6% based on total COD (TCOD), whereas those of ASP were between 87.4+/-1.8% and 90.3+/-0.8%. The contribution of the membrane in the increase in performance was due to total suspended solid retention and also partly due to retention of proteins and polysaccharides of the sludge supernatant. No significant difference in excess sludge production was observed between the two processes operated at the same SRT, but sludge production in SMBR decreased from 0.31 to 0.13 g(VSS)g(COD)(-1) as SRT increased from 9 to 110 days. The difference in sludge characteristics and performance was especially pronounced as SRT increased, resulting in deterioration of sludge settleability and effluent quality of the ASP (filamentous bacteria, increase of protein and polysaccharide release). Membrane filtration induced accumulation of soluble and colloidal proteins and polysaccharides which were progressively degraded in the supernatant as the SRT increased. At similar SRT, no significant difference was observed in the amount of extractable exocellular polymeric substances (bound EPS) from ASP and SMBR sludge. However as the SRT increased, the total specific amount of bound EPS in flocs decreased and the ratio proteins/polysaccharides also decreased. Concomitantly, laser diffraction analysis, microscopic observations, turbidity and DSVI measurement showed that the SRT increase induced significant modifications in sludge morphology in SMBR: decrease in floc size, densification of aggregates, and development of non-flocculating organisms.  相似文献   

7.
Two identical bench scale inclined plate membrane bioreactors (ip‐MBRs) were operated for the treatment of real municipal wastewater for 1 year. Sludge retention time (SRT) was varied over the course of operation to investigate the effects on inclined plate function, treatment performance and sludge characteristic. Removal rates of chemical oxygen demand and ammonia over 90% and of total nitrogen (TN) more than 70% were achieved when ip‐MBRs were operated under SRTs between infinite and 40 days while short SRT (20 days) negatively affected TN removal. When the sludge concentration in anoxic tank exceeded 15 g/L, the failure of the inclined plate function was observed, resulting in no difference in sludge concentrations between aerobic and anoxic tanks. To avoid severe effects on inclined plate function and treatment performance, an SRT range of 40–80 days was recommended for ip‐MBRs. Moreover, sludge floc size under prolonged SRT became smaller than that under short SRT due to increased attrition among the sludge floc particles caused by strong aeration needed for keeping a sufficient dissolved oxygen level.  相似文献   

8.
Performance of laboratory scale completely mixed activated sludge reactors fed with abattoir wastewater was measured at different dissolved oxygen (DO) concentrations. Degradation of fat present in the influent was inhibited at DO concentrations below about 0.5 mg l−1, leading to sludges with high fat content which settled poorly due to excessive numbers of filamentous microorganisms. Fat was degraded rapidly at higher DO concentrations (up to 4.0 mg l−1) and the sludge contained few filamentous microorganisms, a low fat content and settled readily. However, effluent quality was highest at low DO concentrations due to lower levels of soluble breakdown products from the fat.When wastewater was fed intermittently at constant aeration rate, sludge with a low fat content and good settleability resulted, even though the DO concentration was about 0.2 mg l−1 for more than 30% of the time. Effluent quality was also high. Thus it is concluded that for full-scale abattoir treatment plants where wastewater flow is intermittent, DO concentration may be low during periods of high loading without adversely affecting effluent quality or sludge settleability.  相似文献   

9.
An aerobic granular sludge (AGS) reactor was run for 280 days to study the competition between Phosphate and Glycogen Accumulating Organisms (PAOs and GAOs) at high temperatures. Numerous researches have proven that in suspended sludge systems PAOs are outcompeted by GAOs at higher temperatures. In the following study a reactor was operated at 30 °C in which the P-removal efficiency declined from 79% to 32% after 69 days of operation when biomass removal for sludge retention time (SRT) control was established by effluent withdrawal. In a second attempt at 24 °C, efficiency of P-removal remained on average at 71 ± 5% for 76 days. Samples taken from different depths of the sludge bed analysed using Fluorescent in situ hybridization (FISH) microscopy techniques revealed a distinctive microbial community structure: bottom granules contained considerably more Accumulibacter (PAOs) compared to top granules that were dominated by Competibacter (GAOs). In a third phase the SRT was controlled by discharging biomass exclusively from the top of the sludge bed. The application of this method increased the P-removal efficiency up to 100% for 88 days at 30 °C. Granules selected near the bottom of the sludge bed increased in volume, density and overall ash content; resulting in significantly higher settling velocities. With the removal of exclusively bottom biomass in phase four, P-removal efficiency decreased to 36% within 3 weeks. This study shows that biomass segregation in aerobic granular sludge systems offers an extra possibility to influence microbial competition in order to obtain a desired population.  相似文献   

10.
Bench scale activated sludge reactors with a solids retention time of 9 days were operated at all combinations of two levels of pH, dissolved oxygen (DO) concentration and feed type (pH 6 and 8; DO 1 and 7 mg 1−1; simple and complex feed). Long-term composite samples were collected and adjusted to neutral pH and equal concentrations of alkalinity and ammonia nitrogen. They were then breakpoint chlorinated with NaO36Cl in order to determine how much chlorine was incorporated into the organic matter. The amounts ranged from 0.019 to 0.067 mg atomic chlorine incorporated per mg soluble organic carbon. Analysis of variance revealed that the DO concentration was the only independent variable to have a significant effect upon the amount of chlorine incorporated, with reactors operated at high DO levels generally producing effluent organics which were less susceptible to adding chlorine.  相似文献   

11.
Increasing system closure in paper mills and higher process water temperatures make the applicability of thermophilic treatment systems increasingly important. The use of activated sludge as a suitable thermophilic post-treatment system for anaerobically pre-treated paper process water from a paper mill using recycled wastepaper was studied. Two lab-scale plug flow activated sludge reactors were run in parallel for 6 months; a thermophilic reactor at 55 degrees C and a reference reactor at 30 degrees C. Both reactors were operated simultaneously at 20, 15 and 10 days SRT. The effects of temperature and SRT on sludge settleability and chemical oxygen demand (COD) removal efficiencies of different fractions were studied. Total COD removal percentages over the whole experimental period were 58+/-5% at 30 degrees C and 48 +/- 10% at 55 degrees C. The effect of the SRT on the total COD removal was negligible. Differences in total COD removal between both systems were due to a lesser removal of soluble and colloidal COD at 55 degrees C compared to the reference system. At 30 degrees C, colloidal COD removal percentages were 65+/-25%, 75+/-17% and 86+/-22% at 20, 15 and 10 days SRT, respectively. At 55 degrees C, these percentages were 48+/-34%, 40+/-28% and 70+/-25%, respectively. The effluent concentrations of colloidal COD in both systems were related to the influent concentration of colloidal material. The thermophilic sludge was not able to retain influent colloidal material as well as the mesophilic sludge causing a higher thermophilic effluent turbidity. Sludge settling properties were excellent in both reactor systems. These were neither temperature nor SRT dependent but were rather caused by extensive calcium precipitation in the aeration tanks creating a very dense sludge. For application in the board industry, a thermophilic in line treatment system seems feasible. The higher effluent turbidity is most likely offset by the energy gains of treatment under thermophilic conditions.  相似文献   

12.
溶解氧浓度对A~2/O工艺运行的影响   总被引:2,自引:0,他引:2  
以城市污水厂中最常采用的A2/O工艺为研究对象,开展了处理实际生活污水的研究,系统探讨了DO浓度对该工艺运行的影响。结果表明,当好氧区的DO平均浓度从4.0 mg/L降低至1.0 mg/L时,对COD的去除基本不受影响;而系统的硝化效果逐渐降低,但是低DO浓度引发的SND等作用,使得对TN的去除率反而逐渐升高。单纯从生物脱氮的角度考虑,A2/O工艺可以在DO为1.0~2.0 mg/L之间运行。不过低DO浓度运行对生物除磷效果的影响很大,在DO为1.0 mg/L时,除磷效率逐渐下降,这是由于供氧不足引发了生物除磷性能的恶性循环。另外,低DO浓度运行还引发系统中的污泥发生了微膨胀现象,在污泥微膨胀期间出水SS<5 mg/L。就总体的运行情况而言,不同于A/O等单纯脱氮工艺,A2/O工艺不宜在DO<2.0 mg/L的条件下运行,否则需要引入化学除磷。  相似文献   

13.
The specific solid retention time for different bacteria within flocculent and granular sludge was determined. Samples were collected from reactor and effluent sludge and the number of a specific bacterial group was evaluated in respect to the total bacterial community with quantitative polymerase chain reaction (qPCR). The ratio of the relative presence of a specific bacterial group in the reactor sludge and wasted sludge was established to observe if preferential wash-out occurred. From the data also the solid retention time for different microbial groups can be estimated. Using this tool, we were able to show that the SRT of populations found on the exterior of granules is slightly lower than the SRT for population in the interior. Archaea were not found in the flocculent system but were present in small amounts within the granular system. It was further observed that protozoa were grazing on the bacterial community within the system indicating that they have the potential to shorten the specific SRT of bacteria.  相似文献   

14.
The effect of operating conditions on aquatic worms eating waste sludge   总被引:3,自引:0,他引:3  
Several techniques are available for dealing with the waste sludge produced in biological waste water treatment. A biological approach uses aquatic worms to consume and partially digest the waste sludge. In our concept for a worm reactor, the worms (Lumbriculus variegatus) are immobilised in a carrier material. For correct sizing and operation of such a worm reactor, the effect of changes in dissolved oxygen (DO) concentration, ammonia concentration, temperature and light exposure were studied in sequencing batch experiments. DO concentration had an effect on both sludge consumption rate and sludge reduction efficiency. Sludge consumption rate was four times higher at DO concentrations above 8.1 mg/L, when compared to DO concentrations below 2.5 mg/L. Sludge reduction was 36 and 77% at these respective DO concentrations. The effect is most likely the result of a difference in gut residence time. An increase in unionised ammonia concentration drastically decreased the consumption rate. Ammonia is released by the worms at a rate of 0.02 mg N/mg TSS digested; therefore, replacing the effluent in the worm reactor is required to maintain a low ammonia concentration. The highest sludge consumption rates were measured at a temperature around 15 °C, whilst the highest TSS reduction was achieved at 10 °C. Not exposing the worms to light did not affect consumption or digestion rates. High temperatures (above 25 °C) as well as low DO concentrations (below 1 mg/L) in the worm reactor should be avoided as these lead to significant decreases in the number of worms. The main challenges for applying the worm reactor at a larger scale are the supply of oxygen to the worms and maintaining a low ammonia concentration in the worm reactor. Applying a worm reactor at a waste water treatment plant was estimated to increase the oxygen consumption and the ammonia load by 15-20% and 5% respectively.  相似文献   

15.
高硫化物型污泥膨胀的形成机理与控制   总被引:1,自引:0,他引:1  
对含硫酸根的高浓度工业废水在好氧曝气池中产生高硫化物型污泥膨胀的原因进行了分析。在复合式生物反应器中,采用DO—pH控制法对高硫化物型污泥膨胀进行控制,试验结果表明,通过调整进水pH值来控制污泥膨胀的方法经济有效且简便易行。在缺氧条件下,将进水的pH值提高至7.5时,出水SVI值由834 mL/g降至200 mL/g;在微氧状态下,保持pH值为7.5,并将生物选择器调至DO=0.7~1.0 mg/L时,SVI值快速降至100 mL/g以下。  相似文献   

16.
Chua AS  Takabatake H  Satoh H  Mino T 《Water research》2003,37(15):3602-3611
In this paper, the production of biodegradable plastics polyhydroxyalkanoates (PHA) by activated sludge treating municipal wastewater was investigated. The effect of three operational factors, i.e. the acetate concentration in influent, pH, and sludge retention time (SRT) were studied. Sludge acclimatized with municipal wastewater supplemented with acetate could accumulate PHA up to 30% of sludge dry weight, while sludge acclimatized with only municipal wastewater achieved 20% of sludge dry weight. It was found that activated sludge with an SRT of 3 days possessed better PHA production capability than sludge with an SRT of 10 days. Sludge acclimatized under pH 7 and 8 conditions in sequencing batch reactors (SBRs) exhibited similar PHA production capability. However, in PHA production batch experiments, pH value influenced significantly the PHA accumulation behavior of activated sludge. When pH of batch experiments was controlled at 6 or 7, a very low PHA production was observed. The production of PHA was stimulated when pH was kept at 8 or 9.  相似文献   

17.
In this paper, a simulation benchmark of a pre-denitrifying activated sludge process is utilized in order to evaluate a supervisory aeration volume control strategy. The aeration volume control strategy has also been evaluated in a pilot plant at Hammarby Sj?stad in Stockholm, Sweden. The main idea has been to let the dissolved oxygen (DO) concentration in some of the aerated compartments be determined by a higher level controller driven by the DO concentration in other compartments. In this way, only sensors for measuring the DO concentrations are needed for the decision of time varying DO set-points. The high reliability of such sensors implies robust input values for the proposed control strategy. Moreover, it is known that the respiration rate is affected by the content of substrate and nitrogen in the compartments; therefore, the suggested manipulations of the DO set-points are indirectly determined by the current load into the plant. Compared to constant DO control and a supervisory DO set-point control strategy based on ammonium measurements in the last aerobic compartment, the suggested aeration volume control strategy could reduce the effluent nitrate and ammonium concentrations significantly without increasing the aeration energy.  相似文献   

18.
Micropollutants as endocrine disrupting compounds (EDC) or pharmaceuticals are of increased interest in water pollution control. Wastewater treatment plant (WWTP) effluents are relevant point sources for residues of these compounds in the aquatic environment. The solids retention time (SRT) is one important parameter for the design of WWTPs, relating to growth rate of microorganisms and to effluent concentrations. If a specific substance is degraded in dependency on the SRT, a critical value for the sludge age can be determined. In WWTPs operating SRTs below this critical value, effluent concentrations in the range of influent concentrations or a distribution according to the adsorption equilibrium have to be expected, whereas in WWTPs operating at SRTs higher than the critical value degradation will occur. Critical SRTs were determined for different micropollutants, indicating that the design criteria based on the sludge age allows an estimation of emissions. Different treatment technologies as conventional activated sludge systems and a membrane bioreactor were considered and no significant differences in the treatment efficiency were detected when operated at comparable SRT. The results of the investigations lead to the conclusion that low effluent concentrations can be achieved in WWTPs operating SRTs higher than 10 days (referred to a temperature of 10 degrees C). This corresponds to the requirements for WWTPs situated in sensitive areas according to the urban wastewater directive of the European Community (91/271/EEC) in moderate climatic zones.  相似文献   

19.
Bouzas A  Ribes J  Ferrer J  Seco A 《Water research》2007,41(4):747-756
A primary sludge fermentation-elutriation pilot plant was operated using in-line and side-stream schemes. The influence of solids retention time, recirculation sludge flow-rate and solids concentration on the fermentation-elutriation process performance has been assessed in this paper. The use of high elutriation flows (12% of influent flow) improved the volatile fatty acids (VFA) concentration in the effluent stream. Suspended solids removal efficiency decreased in the primary settler when the solids retention time (SRT) was increased from 4 to 8 days. Disintegration step during hydrolysis process was pointed out as the main reason for that decrease. Maximum VFA productions were achieved at SRT between 6 and 8 days at the highest elutriation flow tested for both configurations. Propionic, butyric and valeric volatile fatty acids percentage increased when total solids sludge concentrations above 23,000mgl(-1) were used. Hydrogen accumulation, causing acetogenic bacteria inhibition, was indicated as the reason for C(3)-C(5) fatty acids accumulation.  相似文献   

20.
The general aerobic activated sludge model including nitrification for processes treating principally municipal wastewater is applied to the contact stabilization process treating municipal wastewaters. The application involves two changes to the model: (i) a change in one of the values of the kinetic constants in the expressions of the substrate utilization rates; (ii) a change in the enmeshment mechanism by accepting that a fraction of the particulate COD which is not adsorbed onto the active organisms, does not become enmeshed in the sludge flocs and escapes with the effluent. Accepting only these changes it was found possible to satisfactorily simulate the behaviour of the contact and stabilization reactors of the process under both constant and cyclic conditions of loading.

For design, the general activated sludge model, as applied to the contact stabilization process, requires the process, configuration to be completely specified. To aid in the initial design of the process, a preliminary design procedure is presented by means of which the volumes, sludge concentrations and retention times of the contact and stabilization reactors may be determined from five independent parameters which are assumed to govern the process. These are the sludge age, recycle ratio, fractional distribution of the sludge mass between contact and stabilization reactors, daily COD mass load and the average sludge concentration in the process.  相似文献   


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